Analysis on construction response of the metro mining station adjacent to existing structure
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摘要:
以北京地铁15 号线奥林匹克公园站近接既有隧道结构为工程背景, 采用三维数值模型对其施工响应进行分析和动态模拟, 并与现场实测进行对比, 可得以下结论: 上部小导洞开挖引发的地表沉降占总位移的69.3%, 为暗挖车站近接既有结构施工的关键步序; 上部小导洞开挖建议采取超前注浆加固、缩短开挖进尺、及时施作桩顶冠梁及钢管柱等; 地表沉降最大值位于暗挖车站中线部位, 影响范围为车站中线两侧约40 m; 暗挖车站施工完成后, 既有隧道结构竖向位移最大值为11.06 mm, 满足规范安全要求。
Abstract:
Taking the Olympic Park station in Beijing 15 line as the project background, the dynamic simulation of the existing structure down-traversed by subway station is performed by 3D numerical model vs. site measurement. The results show that: the rate of upper small pilot tunnel excavation is 69.3% of the total surface subsidence, the upper small pilot tunnel excavation is a key step in the existing structure down-traversed by subway station of subsurface excavation station; The suggestion measures are advanced grouting, short footage and tough supporting; crown beam on pile and steel-pipe column applied timely; the maximum surface subsidence is located at the station midline, the range of influence is 40 m at the station both sides; after the subsurface excavation completed, The maximum vertical displacement of the structure of existing tunnel is 11.06 mm and is meet the requirement of Technical code of maintenance for city bridge.