Analyses loss of lock-stress on the prestressed anchor in the anchor-pile and technique improvement
DOI:
CSTR:
Author:
Affiliation:

Clc Number:

Fund Project:

  • Article
  • |
  • Figures
  • |
  • Metrics
  • |
  • Reference
  • |
  • Related
  • |
  • Cited by
  • |
  • Materials
  • |
  • Comments
    Abstract:

    There were great difference between actual results of Shijiazhuang deep foundation pres-tressed anchor and theoretical calculations results, the retaining structure monitoring results an under-ground garage pile-anchor were analyzed.Montitoring results show that the loss prestressed bolt loc-king force is great by using of Native craft methods; the locked stable rally general is only 100kN, which is 1/2 to 1/3 of the original design value.The growth of rally is not obvious according to thelong-term observation results.This paper greatly reduces the loss of the locking force through the ap-propriate technology and construction tools.

    Reference
    Related
    Cited by
Get Citation

CHENG Jian-chun, YE Hong-dong, WEI Dong. Analyses loss of lock-stress on the prestressed anchor in the anchor-pile and technique improvement[J].,2012,29(3):41-44

Copy
Related Videos

Share
Article Metrics
  • Abstract:
  • PDF:
  • HTML:
  • Cited by:
History
  • Received:May 12,2012
  • Revised:
  • Adopted:
  • Online: January 12,2015
  • Published:
Article QR Code